While i do agree that mustang dynos read lower, i don't think is quite that much of a difference.
The spiking of the boost is what killed it , how can you go from 10.5 psi to 15 that is a big difference. Bad tune? Too much Air ?
it didn't go from 10.5 to 15lbs, the 75mm pulley is suppose to make 10.5lbs but with me tune & set it makes 15lbs. & it is 15lbs instant when you hit the throttle. it let go around 4500rpm where peak torque is. plus it was 30 degrees outside.
Tune was spot on, a/f stay at 11.5-11.6, I have aeroforce interceptor setup to tell me if it gets to lean at 5000rpm up, yes its on 93 pump with 15* timing down low & 13* timing up top.
Block or stock internal just couldn't handle the power, car lasted 6000 miles this way, like I said I knew I was pushing it.
I think the guy that broke on the Autobahn said that he did a downshift and floored it and it let go......is that along the same lines of what happened to you?
Who's there?Weren't you having knock issues a while back and your tuner desensitized your knock sensor?
Who's there?