Same rod probably punched two holes. When it breaks the remaining rod on the crank tries to saw the block in two.
That's a great visual.
Guess we'll know more when the heads come off
Same rod probably punched two holes. When it breaks the remaining rod on the crank tries to saw the block in two.
9 pages and still no really good picks of the carnage? I feel for ya op. The original title was a bit off and made people judge this book by it's cover. I think I would of home about this a different route and spoke directly to Shaun or my close mustang buddies before I leaked this on the inter web. But sometimes stuff like this is good because you learn things, 1. Shaun is still an awesome tuner with kick ass customer service. 2. Data logs are important and 3. That guy Hemi lol loves beefcake to death and supports him to the end but runs a BAMA tune. <<< hmmmmmmmmm
But serious note, we've all been here I've popped a few motors and Trans back in the LS days the key is to make it stronger and faster and keep having fun and learn from our mistakes.
And I have an aed e85 tune with a full bolt on cj intake car and Shaun tuned mine it took a while to data log but the car runs like a beast.
Since you have 2 busted cylinders, is it safe to say it's not an injector failure? Sure, one could go out, but the chances of 2 failing at the exact same time is pretty...rare
What are the other possibilities?
Had me scratching my head also. I have a few other ideas in my head. But I'll just wait to see what everything looks like taken apart.
Same rod probably punched two holes. When it breaks the remaining rod on the crank tries to saw the block in two.
Jayvee,
I feel your pain last year getting the car dynoed clutch stuck to the floor on final pull. Pulled of the floor went to drive car home 2 miles later sounded like I shit the trans. So went out bought mangnum swap during the tear down found out the clutch center ring was torn and trans was alright so sold the trans for peanuts and been chasing TOB/slave issue for months finally got it straightened out but now have vibration problem which is either pinion angle or need to get drive shaft checked. Moral to my story went in for a simple dyno pull now spent 7k in parts and install and still chasing my tail. It happens and made me sick to my stomach but in the bigger picture small potatoes I have built motor ordered and once I get the driveline straight will turn up the boost. Take the lemons and make lemonade!
Colin's thought is over-reving. But even that, these motors on stock block have been tested above my shift poit @ 7500. His OTHER theory is, me shifting make to 1st from 2nd meaning to go to 3rd... I looked at him with a face :mj::fm::cuss::nono::shrug: And this is just hime speaking his mind since he also hasn't seen such carnage from a all motor. So... yeah :rollseyes
Colin's thought is over-reving. But even that, these motors on stock block have been tested above my shift poit @ 7500. His OTHER theory is, me shifting make to 1st from 2nd meaning to go to 3rd... I looked at him with a face :mj::fm::cuss::nono::shrug: And this is just hime speaking his mind since he also hasn't seen such carnage from a all motor. So... yeah :rollseyes
By the pic it does look like the piston was broken from the bottom. (like a bullet thru glass)
I was not expecting that.
Time to look for evidence of a seized piston in the bore.
Definitely rod came thru the bottom. You can see the ring which came up when forced from the bottom. Broken rod is the definite cause of the piston.
Why did the rod break? Doesn't look over revved. The tensile strength is compromised over revving and the piston breaks at the top of the cylinder on the exhaust stroke. Then the valves and piston show damage from collision. Don't see that here. Not completely impossible, but unlikely because of other evidence. Seriously doubt it was cylinder pressure that bent/broke a rod. Just not enough power. Hydraulic lock could have definitely bent the rod. An injector could have caused that, which could have lifted the head and let the coolant in. Or a coolant leak could have been the main cause. That will be easier to tell when the injectors are flowed. Rod bends at top dead center and heads back down. With a bent rod, its length is now shorter. Too short to clear the crank counter weight at bottom dead center. Crank smacks the the underside of the piston at the wrist pin and breaks rod. That's why the piston is there, and not at the very bottom of the bore. Breaks at bottom, rod smashes thru it, moves it up a bit.
There is enough remaining piston to see if it hit the crack. If the rod bent the big side will not pin free on the crank likely. Bent rods don't bend one way. They also like to bend and bind the bearing. This may have happened so fast there is no discoloration from heat or lack of oil. But might see some deformation in the bearing. Or, remaining rod in the pan might be obviously bent. So some other stuff to look for to confirm a bent rod is why it broke. Or tell us it wasn't bent.
So it doesn't look like it leaned out or detonated. Detonation could have lifted the head and started the chain reaction, but heads show no sign and neither does the piston. Still like to see the plugs, but sure they look fine. Some of the other stuff I mentioned is still possible, but hard to tell from here and seem very unlikely. But looks like a mechanical issue and not tune related. Sorry about your luck. Seems to to be one of those "Well shit" moments that couldn't be predicted.
Aftermarket tune/ Injectors = Ford giving you finger