Project "Save-A-Fox". Kept this one out of the junk yard...(long post)

FISHTAIL

Will Work For Mods
Established Member
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Messages
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LaPlata, MD
Well guys, this post has been a few months in the making, and is going to be a looong one, with lots of pictures.

So, as some of you know (especially the ones that I'm friends with on FB) I bought a fox convertible last summer as a
project car that I intended to flip after completion to fund parts for the GT. But...for multiple reasons, we have decided to keep it.

That's the basic jyst of it, but the interesting part is the project itself, and thus, story time;

As with most trashed project cars, this story starts with craigslist. Originally, the seller was asking 2k for this car, and
in all of the pictures he had posted, there were none of the interior and in all the exterior shots, the car was wet.

I knew these were red flags, but since the seller was so close (15 minutes away) I decided to go have a look anyway. He'd mentioned in the ad that the car had a tap, so I brought my stethoscope with me when I went to check the car out. As the man said, the car DID have a nasty tap, but I was able to determine pretty quickly that the issue was in the top end. When I told him that, he informed me that he'd recently replaced the main bearings, himself, in the driveway, without pulling the motor, because he thought that *might* be where the noise was...and was surprised when that didn't work. uh oh. lol. Even in the rain, i could tell the paint was severely oxidized, and after glancing inside, I immediately decided the car wasn't worth anywhere close to 2k.

He asked if I wanted to make an offer, I told him no, but to contact me later after he'd had a few, or none..knowing damn well that he was going to end up with the latter. After a couple of weeks, he emailed me back and negotiations started. For reasons I won't post publicly, the guy was able to appeal to my softer side and I agreed to give him 800 for the car..which, as I even told him, was still more than the car was worth.

Still, at the time I was hopeful that I could salvage most of it and make a decent profit so I went ahead and bought the car.

And that is where the fun started. The fellow I got this car from was a very, very kind man, but is one of those people that should be barred for life from ever attempting to turn a wrench again. Everything, and I mean EVERYTHING this guy touched on this car, he screwed up.

First, he'd told me that he was "restoring" the interior. If what I got was restored, I'm horrified to think what it looked
like to start with. When i got this thing, the interior was so disgusting i wouldn't even sit in it with clean clothes on.
The carpet had mushrooms growing out of it, the door panels were white, the map pockets were grey, and the door handles were red. The front seats were brown (SN95), and the rear were destroyed original white leather. The center arm rest was gone, the passenger rear interior panel was broken in half (which I didn't notice right away because of how he had it sitting), the radio was half out, and there were pepboys "accessories" screwed into the dash, center console and random shit everywhere. In short, it was an unmitigated disaster. I don't have any pictures of this because it stayed like that for all of a couple hours before I started ripping shit out and throwing in the garbage. I never really intended to document it..just fix it. The paint was so badly oxidized that the car had a white hue to it, the paint was flaking off the wheels, and the top was covered in mildew.

WTF i was thinking..I'll never really know. I like a challenge I guess.

This post is already getting long in the tooth, so rather than explain how I came to find everything, I'll just list what I found (andcan remember) offhand for everyones amusement;
The passenger rear 1/4 window had broken the torque pins in the motor and was stuck (regulator rusted in place) about 3/4 of the way up. This is how water got in, the mushrooms grew, and how the rear panel was broken in half. The guy couldn't find the screws apparently, so he just broke the panel to remove it. Then when he couldn't figure out what was wrong, he reassembled the window guide upside down and left it like that.

I replaced the torque pins in the motor and was able to work the regulator free..window works great now. 2.95 to fix. And he ruined half the interior because of it.

The mildew on the top I was able to remove with a good scrub and some dawn dish detergent. It's still not perfect, but it's not bad either..although the car could use a black top now. The paint I was able to partially salvage, but was so far gone in places that we ended up just painting the car. Even with a PC, I still burned clean through to primer on the first pass in 2 spots, and in others the clear was pitted so badly that polishing the oxidation out almost made it look worse. After about 12-16 hours of working the oxidation out, I threw in the towel and owned up to having to pay for paint.

The engine, as it turned out, was almost totally sludged up. The tapping was the sound of at least 4 broken rockers. Given the other things this guy did (that I'm about to share), and knowing that he'd replaced some bearings in the bottom end (likely only half of them), I wrote the engine off and grabbed another from CL for 400 bucks.

The driveshaft had 3 of the 4 bolts at least halfway out. All finger tight. The speedo sensor was shoved so far into the trans that the gear got held in place and stripped. Then they put the hold down bracket on upside down and broke the bolt off in the transmission. To prevent a leak, the spedo sensor was held in with a coat hanger.

There were 3, yes 3, sets of foglights on the car. All wired horribly. The drivers door hinge pins were shot, but instead of fixing those he adjusted the window stops so the window would "shut". This caused some issues...

The brakes were all new, but the rears were installed backwards and as a result, the self adjusters stripped themselves out and the car made terrible, terrible sounds when the brakes where hit.

The radio was wired incorrectly and didn't work, the car had "light up flame" pep boys pedals on it, and he also managed to destroy the rear view mirror base because he couldn't figure out how to get it off the button.

The passenger front seat was NOT bolted down tightly, at all, and the left front bolt didn't even catch a thread. The drivers front was worse and even had a broken corner, so it was only actually attached to the floor in 3 places rather than 4. Thank god I didn't drive it home, getting in an accident would have been a guaranteed ejection from the vehicle.

And that's just the stuff that comes to mind right away...there was more..much more. I ended up putting far more time into fixing some of the most ignorant stuff I've ever seen someone try than I barganed for. But, it's fixed..mostly. I still have a few little things left to button up, but for the most part, the car is salvaged.

So, in short, here is what I did:
Replaced the engine
Spent about 12-16 hours or so buffing the paint before giving up and getting the entire car painted (Redfire)
Painted the wheels/trim
Gutted the entire interior. Fixed the wiring, re-dyed all the panels, replaced the two rear panels, installed a light bar, and got "new" seats/carpet.

This entire process took probably around 4 months of working in the evenings.

And with that...I shall present you with pictures!

Arrival day after it's first extensive dawn bath:
arrival4_zps170d91f4.jpg

arrival3_zps3dbc68d3.jpg

arrival1_zpsb641c287.jpg

arrival2_zps74e29707.jpg



Attempting to clean up the paint:
pre_buff1_zps4f7b5848.jpg

oxidation2_zps1b707abc.jpg

test_section_zps0b165be1.jpg

pitted_paint2_zpsba32aa38.jpg

oxidation_zps1ee00623.jpg

pitted_paint_zps1e3853fb.jpg

mid_buff7_zps3d96f115.jpg

mid_buff4_zps73d098a5.jpg

mid_buff5_zps2838773e.jpg

mid_buff3_zps1b30f747.jpg

mid_buff2_zps9ae6a277.jpg

mid_buff1_zps84745aaa.jpg

bad_paint_zpsfb1aa01f.jpg

dent_zpsfffddf75.jpg


Engine Replacement:
original_engine_trashed1_zpsa3b7ac2e.jpg

original_engine_trashed2_zps4644673c.jpg

engine_swap_zps5c4cbd57.jpg


What pics I have of the interior when I started:
mushrooms_zpsac9f3f41.jpg

interior_disassembly6_zps6e4660d6.jpg

interior_disassembly5_zpse342b28b.jpg

interior_disassembly2_zpscd8af355.jpg

interior_disassembly3_zps86fcaaff.jpg

interior_disassembly_zps25dd0ada.jpg

interior_disassembly4_zps0cf00eef.jpg

interior_assembly6_zps6e43b038.jpg

floor_rusted_zpsa101483b.jpg



Trashed wheels:
wheel_before2_zps863edbdc.jpg

wheel_before_zpsdc1e497b.jpg


So..as you can see, the car was, well, rough.

I have basically zero pictures of the actual refinishing process, but I have a few of it going back together:
dash_after_zps58e069e1.jpg

console_after_zps5976ddf6.jpg

interior_assembly5_zpsb8afa322.jpg

interior_assembly4_zps36396817.jpg

interior_assembly3_zps5233e985.jpg

inteior_assembly2_zpsdbc823a8.jpg

interior_assembly1_zps56ea7de2.jpg

interior_after2_zps90f3f5d6.jpg

light_bar_zps0e9df3ec.jpg

vert_interior1_zpsfb0af1c5.jpg


How it looked when I dropped it off for paint:
pre_paint3_zpsa9a215c0.jpg

pre_paint2_zps3a9be6a4.jpg

pre_paint1_zpsf3503029.jpg

pre_paint4_zps285fb3b0.jpg



Back from paint:
first_day_back_zps43f4452e.jpg


Repainting the wheels:
caps_before_zps20a8eb26.jpg

caps_inprogress_zps203b9e34.jpg

caps_after_zpse42dba97.jpg

wheelsafter_zpse7e36d1e.jpg


Sanded the rust out of the tails..the un-finished area is how the whole pipe looked:
exhaust_before_zpsca6452e0.jpg

exhaust_after_zpsdd07c225.jpg


How she looks now:
vert_topuprear_zpscaec49fd.jpg

vert_rearqtr_zps2338936a.jpg

vert_topup2_zpsb402eee8.jpg

vert_topup_zps8a6a827c.jpg

vert_passfront_zps07e66d68.jpg



At home:
vert_overall_zps72074294.jpg


First ride:
jon_wave2_zps3cbbdf94.jpg

jon_wave_zps8c203f8a.jpg
 

FISHTAIL

Will Work For Mods
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Messages
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LaPlata, MD
Actually turned out nice..... Good save kind sir!

Thanks! I'm happy with how it turned out so far. I have a short mod list for it, but it's mostly suspension and chassis stiffening stuff..my plan is to keep it stock power wise and just enjoy it.

Given how it started, and how much was just flat wrong on the car, I wasn't sure how it'd turn out..but I think it's safe to say this one won't be hitting the junkyard anytime soon.
 

SC Heaven

Red Whine
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Sep 27, 2012
Messages
863
Location
Colorado
It is mind boggling to me at how bad people can let cars get. Excellent restoration. :beer:

Out of curiousity, did you cut the oil filter open off the old engine? Looks like that oil had seen 10s of thousands of miles.
 

FISHTAIL

Will Work For Mods
Established Member
Joined
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Messages
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Location
LaPlata, MD
It is mind boggling to me at how bad people can let cars get. Excellent restoration. :beer:

Out of curiousity, did you cut the oil filter open off the old engine? Looks like that oil had seen 10s of thousands of miles.

No, it looked like he'd changed it recently, so I didn't bother. There was no buildup in the pan, it was all up top. The engine is at my friends house so he can rebuild it for his vert (which is sitting in a barn) so I'll get a chance to look it over and see how bad it really is later. And I agree...I have no idea why people let stuff go like that. Is it really that difficult to keep something clean at least? Geez.

Amazing transformation

Thanks.
 

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