After swapping on fresh head gaskets, I got the 408 Fox out to the track on Friday. DA was pretty good, around 500 feet, and I cracked the 10's with a 10.99 @ 118.4. This was on a 1.42 60 foot. The car still felt a little soft and I am still chasing this breakup at 6500 rpm. After this run, the power went away and I could not figure it out until I got it home and looked it over on Saturday. The #4 intake rocker completely fell off. The car was on 7 holes and still running mid-11's @ 114. LOL. It was not rough, just down on power. Also, a compression test revealed numbers all over the map. Leak down showed pretty severe leak past the intake valves. So, I pulled the heads and will have a valve job done. I am also going to replace the springs. I am sure after this, the car will run hard 10's on motor and well into the 9's on the 200 shot.
Still, it was a good run and the launch was great.
Enjoy:
https://www.youtube.com/watch?v=JAp0blnoIf0&list=UUECPEzGAKEB4O9G3T-ImoFA&index=8&feature=plcp
https://www.youtube.com/watch?v=1j6THMe2yDc&list=UUECPEzGAKEB4O9G3T-ImoFA&index=4&feature=plcp
Still, it was a good run and the launch was great.
Enjoy:
https://www.youtube.com/watch?v=JAp0blnoIf0&list=UUECPEzGAKEB4O9G3T-ImoFA&index=8&feature=plcp
https://www.youtube.com/watch?v=1j6THMe2yDc&list=UUECPEzGAKEB4O9G3T-ImoFA&index=4&feature=plcp
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