well long story short i put my car back to complete stock format due to a california state ref appointment i have march 1st, i installed the stock exhaust, removed the KB BAP that was on it, is was landed on the green/yellow wire, hooked up original wire with a butt connector, pressure washed it, went around the block idled for about a good 5 mins in my drive way then suddenly shut off and would never start again. I do have fuel in my fuel lines had my chick turn the key to on while i pushed the shrader valve in on the fuel rail, fuel came gushing out..oddly enough the fuel pump prime sound its making is not the same. the sound sort of fluctuates pitch if you will...mind you it also has a n2mb wotbox that seems to be functioning normal. there is also a wierd sound coming from either the PCM or the wotbox. Do you guys think maybe this is all due to the FPDM being hooked up with a butt connector or some sort of short due to pressure washing im totally lost here....its one thing after another