Delving Deeper into the stall/idle issue...

GreyCobra_03

Lurch
Established Member
Joined
Aug 25, 2002
Messages
774
Location
Medford Oregon
Ok, for those of you who haven't seen my posts on the problems with stalling and idle problems, I'll give you a little recap. WARNING: THIS POST MAY BE LONG :)

My car started stalling at about 6000 miles. I had the 1st Gen Densecharger, 2.93 pulley, NGK plugs gapped by Terry at SFPHQ, and a Tri-Ax shifter. The stalling happened on deaccelleration, and seemed to be the typical stall everyone was talking about. I wasn't worried.
I cut out my mufflers (20 HP on the dyno rear wheel for $40) and I installed the AR Diablo Chip. After the chip was installed, I noticed the stall started to get a little worse. I posted on this forum http://svtperformance.com/forums/showthread.php?threadid=36442&highlight=stalling
and recieved some excellent advise. I changed from the Densecharger to an open filter K&N, and tried to follow Larryc7777's instructions on recalibrating the IAC. The stall seemed to lessen, but the idle never really was the same, varying between 720 and 1300 RPM. I figured that the IAC was trying to recalibrate.
Last friday, I was sitting at a stop sign, and I started noticing a little miss while the car was idling. I brought the RPMs up to about 2500 slowly, and heard and felt the misses as the RPM increased. The car's exhaust had been popping and gurgling on deceleration, I figured it was just because I had removed the mufflers. But now I am noticing that it seems to be getting worse and a mechanic out at the track told me the popping is because of either a lean condition or rich condition when I am off the throttle.
I took the car to my friendly neighborhood dyno center, and pulled the plugs and regapped them. BTW, I would highly recomend anyone with "pre-gapped" NGK_TR6s from SFPHQ to recheck their gaps, as my gaps varied from .039 to .048. Terry had told me that the plugs were pregapped to .040.
The A/F ratio on the dyno looked great, all the way through the powerband. With my mods, I pulled 455 RWHP and 470 RWTQ. However, I still had the popping, almost a backfire sound, on deceleration, and the car was still obviously missing.
Can someone help me out with this problem? I have put in a call to Rick at Amazon Racing, I know he will help me out, but I have always recieved excellent advise on this forum. Should I return the car to stock and have Ford reflash the program? Any suggestions?
 

Users who are viewing this thread



Top